Electrostatic Discharge
FREE FOR MEMBERS
Individual membership and corporate sponsorship in the Vibration Institute includes
SPECIAL OFFER!
Become a Vibration Institute Member today for only $95 and get access to the entire document library at no charge.
BUY IT FOR $99
Only interested in this article? You can make a one time purchase to download this content.
Electrostatic Discharge in a Condensing Steam Turbine Driving a Propylene Compressor Train
by Jonathan Cardell and Stephen Plaisance
Abstract
This paper is a case study of bearing damage caused by electrostatic discharge. Many photos of the actual pad damage are given. Many characteristic orbits with the descriptive random spikes caused by electrostatic discharge are shown. An economic evaluation of the potential losses averted is included. Before and after orbits are shown that prove the newly installed grounding brush stopped the progression of the problem. Several references are given in the bibliography of other similar situations.

PREVIEW
“Machine Train Layout:
Figure 1 shows the propylene compressor train that is the subject of this article. A steam turbine drives a Low Pressure (LP) and High Pressure (HP) axial compressor, which are coupled in tandem.
"Machine Characteristics:
"Condition Monitoring System Display:
The System 1 display consoles shown in Figure 2 are located where they are easily accessible by the turbomachinery team.
"Process Upset:
On the morning of 10 April 2009, a process upset following a converter mis-valving event sent the Propylene LP Compressor into severe surge condition (Figure 3).
Initial diagnosis of the event included reviewing the following parameters:
The data reviewed in these parameters did not appear to correlate with the vibration trends. However, the shape of the orbit (Figure 4) in the steam turbine outboard bearing suggested that a rub condition could be present. Figure 5 shows trends of the unfiltered (Direct) vibration amplitudes at the steam turbine bearings.
The decision was made to continue to monitor machine condition with the expectation that the process conditions would stabilize with the proper valve operations set.
We believed that this rub was due to a thermal bow of the rotor on that end of the machine, possibly a “hot spot” on the rotor. We adjusted the balancing steam to pull more flow from the high pressure end of the machine to the low pressure end. This slowed the rate of change in bearing vibration. At this point, we continued to monitor the machine, expecting stabilization.
Vibration continued to slowly trend up (Figure 6), even after waiting for the thermal bow to dissipate. The team began to look at other possible failure mechanisms that could be exhibiting such behavior. The rub was evident, but closer examination showed a continuous degradation in shaft position within the bearing. Having noted this, other previously unseen clues began to surface as suspect.”
Vibration Analysis Certifications
The Vibration Institute Training Courses provide unique opportunities to study vibration principles in a way that goes beyond the textbook to provide real-world applications.
